This repository has been archived on 2022-01-28. You can view files and clone it, but cannot push or open issues or pull requests.
Marlin-Artillery-M600/Marlin
swilkens 06e2afe8e0 [2.0.x] Reduce HOMING_FEEDRATE_XY for Ender 3 (#12105)
Homing on the Ender 3 with HOMING_FEEDRATE_XY set to 50*60 was shown (#12074) to cause the end-stop micro-switches to bottom out, causing the carriage for both X and Y axis to physically crash into the micro switch. Reducing the homing speed prevents the switches from bottoming out.
2018-10-16 01:51:47 -05:00
..
lib Module updates 2017-09-21 16:26:42 -05:00
src [2.0.x] Reduce HOMING_FEEDRATE_XY for Ender 3 (#12105) 2018-10-16 01:51:47 -05:00
Configuration.h Extend M217 with configurable park/raise (#12076) 2018-10-13 23:08:20 -05:00
Configuration_adv.h Option for G0 to have a separate feedrate (#12089) 2018-10-16 01:49:51 -05:00
Makefile Fix "Missing separator" errors. (#12035) 2018-10-08 14:28:52 -05:00
Marlin.ino Marlin.ino needs no content (#9506) 2018-02-06 02:28:18 -06:00